![]() |
She really has come a long way, even with just this year already! |
Showing posts with label Maintenance. Show all posts
Showing posts with label Maintenance. Show all posts
July 14, 2014
Recent Racing Updates
July 6, 2012
Blueberry's Bruise
![]() |
Rotors and Eccentric Shaft freshly removed |
June 8, 2012
Bad Camber Bolts?
![]() |
On the alignment rack |
June 2, 2012
Stuck Swaybars?
![]() |
Dry bushings can't be very helpful I bet |
April 3, 2012
Ti Gri's Engine Bay Overview - Part 1
![]() |
Ti Gri in her full glory! |
March 29, 2012
Build Weekend... Again!
![]() |
Blueberry - 4x4 Status |
Since Blueberry was my daily driver for years in the Northeast, I have one word: Rust. When disassembling the rear, I discovered that my tie rods were not only rusted, but completely frozen solid in place. That is when the RE-Zelse team and Luis from Wankel Works assembled together down in Pennsylvania to help me finish the work I started.
October 1, 2011
Engine Issues Resolved
I was chasing down a "gurgling/fluttering" noise at 8,000RPM for a little over a month recently. The noise was very noticeable and had gotten me very concerned, so I could simply not ignore it. After a lot of digging around and countless times of ripping things apart, I figured out what I was faced with. The interesting part of this however is that not only did I figure out the problem, I learned that I was chasing 3 separate problems. I thought I would share my findings with everyone, just incase someone should run into a similar issue.
August 28, 2011
Whats New?
A lot has been going on the past few weeks, so I'm glad I finally have some time to myself to kick back and relax. The main topics of whats new is in bold below. You will begin seeing more review posts, DIYs, and casual posts now that things are back under control.
The blog has received many changes over the past few nights. Most of these updates I have been planning to implement for awhile. For starters, I decided to spruce up the fonts and colors used around the blog a little bit, while maintaining the same overall feel as before. Then, I cleaned up the side bar by getting rid of a few extra things and making everything easier to navigate. I also added some new pages to my blog that I think everyone will enjoy.
The blog has received many changes over the past few nights. Most of these updates I have been planning to implement for awhile. For starters, I decided to spruce up the fonts and colors used around the blog a little bit, while maintaining the same overall feel as before. Then, I cleaned up the side bar by getting rid of a few extra things and making everything easier to navigate. I also added some new pages to my blog that I think everyone will enjoy.
September 13, 2010
False Alarm

Regardless, Liberty Mazda saved the day and replaced the broken thermostat with a working OEM one. A few test drives and everything was working great. Temperatures are roughly 5 degrees higher now, but fluctuating between the temperatures is minimal. That being said, I think I'll be staying with the OEM thermostat, even though Mazmart is willing to replace it, free of charge. Thanks for saving the day though Liberty, glad that my engine isn't gone and still running strong.
April 12, 2010
Liberty Mazda Visit - Power Steering Be Gone!
Decided to drop off the car early in the morning before work to get looked at. The front accessory socket malfunctioned on Sunday, and the never-ending power steering issues that seem to happen at all the right times. We'll have to see what they say about it all, but I have a feeling it is the only part that was not replaced; the wiring harness.
UPDATE: Got a phone call from the dealership that it is the wiring harness that is malfunctioning. Go figure, the cheapest and easiest part to replace was the cause of all the power steering issues, at least I'm just guessing. Will be picking the car up on Wednesday.
UPDATE: Got a phone call from the dealership that it is the wiring harness that is malfunctioning. Go figure, the cheapest and easiest part to replace was the cause of all the power steering issues, at least I'm just guessing. Will be picking the car up on Wednesday.
March 11, 2010
Liberty Mazda Visit

For starters, they saved a unfinished bodywork job on my trunk and bumper. The results were better than expected, and I wish I just went to them from the start. The trunk is now wingless, and the holes for the badges that I plugged before and the holes for the wing are welded up, all with fresh new paint. Bumper had gotten a little scraped up and badly chipped from all my highway miles, so it needed a repainting for sure.
For maintenance goodies, I got my transmission fluid changed, my differential fluid changed, state inspection, engine compression test, and my new REmedy Oil Pressure Regulator upgrade. Everything went smoothly, big ups to Mike and Tom for their hard work in making sure I'm taken care of. For those who are wondering of the results of my compression test, I think Ray of BHR had said it best,"Dude! Your engine is backwards!"
Front rotor at 250 RPM came out to an average of 8.2. The three runs were 8.6, 7.9, and then 8.1. The rear rotor at 227 RPM came out to an average of 8.6. The three runs were 8.4, 8.6, and 8.9. Most rebuilt engines see high 9 numbers. It's interesting as usually most rotary engines have the rear rotors start failing first, seeing lower compression there instead of the front as the rear rotor runs hotter than the front. But surprisingly with all I have been doing, my 2004 engine with 52,000 miles is running quite strong. No complaints here!
Here are some more pictures of the debadged and dewinged trunk.


December 6, 2009
Prepping For Winter
Getting the car ready for winter can be a bit tricky it seems, as you want to make sure you don't leave anything out. This is the first year the car will be in the garage all winter, so I had spoke to a few people to see what was necessary for proper storage. In short, your list should look something like this.
- Quick Wash
- Oil Change
- Coolant Change
- Top Off Gas Tank with Gasoline Stabilizer
- Park Car on Cardboard Pieces
- Block Off Wheels with Wheel Chocks
- Release E-Brake
- Inflate Tires to 50PSI
- Set Shocks to Full Soft
- Empty Glove Box and Other Compartments
- Place Dryer Sheets in Car to Avoid Musty Smell
- Remove Battery and Connect to Battery Tender
- Block Tail Pipes, Cooling Ducts, etc. with Rags to Keep Animals Out
- Close Windows
- Set Vents to Open
- Cover (If Not in Garage)
- Detail Throughout Winter
November 20, 2009
Issues Fixed!

The power steering rack, as well as PCM (Power Control Module I believe) had to be replaced. Most RX-8 owners usually need their wiring harness or PCM replaced, but a few needed their rack replaced instead. I guess I needed the two! Car feels normal again with no issues, and have driven it a bit before deciding to post this.
My oil pan needed to be resealed again it seems, so they had taken care of that while the car was there. Hopefully this time I won't get any leaking after a couple of months.

A few other Stance owners have mentioned running into this after numerous track events/autocrosses. Luckily, the fix is to simply retighten it. I really didn't feel like getting anything replaced right before the winter or something.
Not much else, but I am looking forward to Jason Isley's article in Sportscar coming up in December regarding his RX-8 setup for STX! Stay tuned for a review of that.
September 17, 2009
More Exhausting Exhaust Stuff!
Was feeling better yesterday and decided to play around with the exhaust for a bit with my buddy James at Oleg's house. We solved a few issues I was having, but created one big one in the end.
As I'm writing this now, just got a call from the dealership (James took the car in for me, big ups to James!) saying that it is all set. Big ups to Liberty Mazda for saving the day as usual! For now, it looks like I'm rattle free and exhaust leak free ( for the most part), but catback less. I think I'll be waiting for the BHR catback, as I have a good feeling about whats to come with it. Stay tuned.
- We tightened the bolts from midpipe to header more and that helped seal the exhaust leak upon startup. It's very minimal now and barely lasts awhile when the car is warming up.
- We were curious if the piece that had broken from the midpipe would be able to come out if we tipped the midpipe or something. Instead, when we took off the OEM Catback..the piece came out from there. No more rattle!
- We tested the HKS Hi Power with this midpipe to see what the volume levels would be like. As awesome as it sounds, with the crackling and popping, especially at redline, it is still too loud.
As I'm writing this now, just got a call from the dealership (James took the car in for me, big ups to James!) saying that it is all set. Big ups to Liberty Mazda for saving the day as usual! For now, it looks like I'm rattle free and exhaust leak free ( for the most part), but catback less. I think I'll be waiting for the BHR catback, as I have a good feeling about whats to come with it. Stay tuned.
September 14, 2009
Exhaust Update
Was at Liberty Mazda today to get my worn engine mounts replaced as well as my old OEM header to be installed again in hopes it'll get quiet and fix the exhaust leak. Engine mounts helped make the car a lot smoother, so that worked out great!
As for the exhaust, it seems I still have a slight leak when it is cold. The flange isn't warped like the other header though luckily, so it could be the old gasket warped due to the previous header. The annoying buzz is gone, and the exhaust is as quiet as stock, so I think I'm going to try the HKS back on the car again in hopes it won't be too loud again. I think it will work out fine, just need to narrow down how to fix the leak, and wait for BHR to release Ver. 2 of their midpipe to get rid of the occasional rattle.
Stay tuned.
As for the exhaust, it seems I still have a slight leak when it is cold. The flange isn't warped like the other header though luckily, so it could be the old gasket warped due to the previous header. The annoying buzz is gone, and the exhaust is as quiet as stock, so I think I'm going to try the HKS back on the car again in hopes it won't be too loud again. I think it will work out fine, just need to narrow down how to fix the leak, and wait for BHR to release Ver. 2 of their midpipe to get rid of the occasional rattle.
Stay tuned.
September 1, 2009
Showing Off The Sponsor

To top it off, we were able to slap on a nice banner from one of my sponsors, Sleepermodz.com. We’ll see how this midpipe turns out, but the idle is great now, and the banner blends in just right!
April 9, 2009
Patch Work

Removing the side skirts was a bit tedious, as it had to be cleaned from the 3M tape and dust. Then we had to plug the holes with "hole plugs" from Home Depot, painted with touch up paint and clear coated, and then some slight super glue around the edge to make sure it is on against the body firmly. Will have more side shots soon.
Bumper was buffed out, again thanks to Josh. Looks brand new, except for the few rock chips, so looks like someone put white out here and there. Headlights needed a serious makeover as well as they were hazed and scratched from the baking we did. Much better with a much better output.
Lastly, the fogs were simple to remove, just 3 screws from the foglight assembly into the bumper and they're off. The PIAA's I had previously were blown, and I had slowly gotten out of the fog light phase, so I removed them.
More pictures can be seen here. Thanks a million to Josh for the help!
March 4, 2009
Maintenance At DSG

Thanks to Nick from DSG for the pictures!


October 14, 2008
Oil Change And Maintenance


My understanding is that the way RedLine oil is made, it has certain properties about it that make it so the apex seals wear and tear much less then normal. And since the viscosity is higher in the oil , as the oil heats up and thins out, it won't be thin to the point that seals could start rubbing against the housing, making this oil one of the best choices. Granted, most tuning companies in Japan are running their own premixture oils of 10w 50, but this will do for now.
I just want to add that after changing my oil and oil filter to this, my engine feels a lot happier and more at home when revving. Before it felt great, peppy and lively, but a slight bit "upset" with small rumbling. Now, when revving the engine, it feels smooth as butter, and I already noticed a slight increase of MPG. Idling is still similar to before as I have done the airbox modification, but it was still noticibly better, by both me and the mechanic. I highly recommend this oil and oil filter to anyone who is serious about maintaning their RX8 to it's fullest, as this really was worth the extra money. I don't know about you readers, but I disagree with using a OEM filter that is used on all of Mazda's cars, as opposed to a special oil filter for a special engine.
September 18, 2008
Bleeding The Clutch
The process sounds a lot easier then it really is. Honest. And sadly, we needed three people to do this job. NOTE: Make sure your car is COOLED DOWN or you WILL burn hair off your arm (I learned the hard way). You start by jacking up the front of the car ( a good amount, one of you 3 is going under there) and setting it on jack stands.
Take off the cover of the brake fluid reservoir. You're going to need a light under the car, as well as above from the hood so everyone can see where the bleeder is. In the picture above, look between the oil filter and the clutch line... That is the bleeder with the rubber cap on. It's really frustrating to reach from both directions, but we managed. Remove the rubber cap, then slip a 8mm wrench up carefully and placed the closed end on the bleeder. This will be a pain, but patience and help from the other person in the hood, you'll be okay. Make sure it's on the bolt tight, then fit on the hose.
When the hose is on perfect, put the other end into a disposable cup or bottle, but clear enough you can see what is going on. Now, someone will have to go into the car and get ready to pump the clutch, while the person under the car will open the bleeder valve, while the third person will be watching the cup for air.
Start off by holding the clutch pedal to the floor, open the bleeder valve, then close. Pick up the pedal from the floor (It'll stay stuck to the floor) and begin to pump it a good amount until you really can't anymore...and then hold to the floor. The person under the car will then open the valve and release more air or fluid. After you've done enough and gotten rid of all the air bubbles and have nothing but fluid constantly coming out, replace the fluid you've gotten rid of and cap everything back together.
Give the pedal a few pumps before driving to make sure it feels good, then after, you should notice a serious improvement. I've read somewhere that you may want to bleed the master cylinder before AND after bleeding the clutch line, but we only bled it after the clutch line. Huge difference to my pedal after doing this.
Subscribe to:
Posts (Atom)